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At about 10:10 am on February 7, 2017, on-site DWR personnel noticed a
substantial disturbance in the service spillway’s flow pattern, while discharges were
being ramped up from about 1,200 m3/s (42,500 ft3/s) to about 1,490 m3/s (52,500
ft3/s). On-site DWR personnel contacted DWR headquarters in Sacramento, and
an order to close the service spillway gates was issued at about 11:15 am on
February 7, 2017. After the gates were fully closed by about 12:25 pm, it was found
that a significant section of the service spillway chute slab was missing, and a large
erosion hole existed in the foundation in the area where the slab sections were
missing, as shown in Fig. 9. This initial erosion hole in the service spillway chute
was examined by a climb team on the morning of February 8, 2017.
Fig. 9
Service spillway chute damage observed after gates
were closed on February 7
DWR knew that it would need to operate the damaged service spillway
because of expected inflow to Lake Oroville; hence, it was decided to begin
opening the spillway gates to test the service spillway’s capabilities in the damaged
condition. The gates were reopened at about 4:00 pm on February 8, 2017, and
several different discharge levels were trialed through February 10, while the
service spillway chute was observed for additional damage. Spillway discharge
reached 1,840 m3/s (65,000 ft3/s) at 3:00 am on February 10, and was held there
for about 17 hours. At about 8:00 pm on February 10, the service spillway
discharge was reduced to about 1,560 m3/sec (55,000 ft3/s) and maintained at that
level through 3:35 pm on February 12.
Meanwhile, inflows to Lake Oroville continued to increase. Sometime
between about 7:00 and 8:00 am on February 11, the reservoir level exceeded
Elevation 274.6 m (901 ft), and water began flowing over the emergency spillway
crest structure for the first time in the facility’s history. The reservoir level increased
to a maximum level of about Elevation 275.1 m (902.6 ft), about 0.49 m (1.6 ft)
above the emergency spillway’s crest, at about 3:00 pm on February 12, about 31
hours after the flow over the emergency spillway began. The flow over the
158
Book of Full Papers
Symposium Hydro Engineering
- Title
- Book of Full Papers
- Subtitle
- Symposium Hydro Engineering
- Author
- Gerald Zenz
- Publisher
- Verlag der Technischen Universität Graz
- Location
- Graz
- Date
- 2018
- Language
- English
- License
- CC BY-NC-ND 4.0
- ISBN
- 978-3-85125-620-8
- Size
- 20.9 x 29.6 cm
- Pages
- 2724
- Keywords
- Hydro, Engineering, Climate Changes
- Categories
- International
- Naturwissenschaften Physik
- Technik